shift1 problem solved

pull/139/head
erikkaashoek 12 months ago
parent ac8db4e46a
commit 73fe677ce8

@ -1262,7 +1262,7 @@ const float v5_2_correction_value[CORRECTION_SIZE][CORRECTION_POINTS]=
/* out */ { 8.37, 5.53, 2.3, -1.37, -3.14, -3.43, -5.06, -5.59, -5.95, -5.59, -4.55, -5.06, -5.06, -5.59, -5.35, -5.78, -5.12, -5.17, -3.81, -2.37},
/* direct */ { -3.9, -2.73, -2.55, -2.5, -1.04, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03, -0.03},
/* adf */ { -3.25, -2.51, -1.77, -1.34, -0.16, 2.8, 5.37, 5.23, 3.76, -0.93, -1.98, -4.71, -5.41, -7.41, -8.63, -8.53, -8.28, -7.66, -7.56, -5.78},
/* ultra */ { 8.24, 4.14, 1.31, -1.56, -3.29, -5.09, -5.59, -4.86, -5.78, -4.61, -4.67, -2.02, -2.93, -0.36, 2.78, 1.84, 4.97, 8.07, 11.98, 11.47},
/* ultra */ { 8.24, 4.14, 1.31, -1.56, -3.29, -5.09, -5.59, -4.86, -5.78, -4.61, -4.67, -2.02, -2.93, -0.36, 2.78, 1.84, 4.97, 8.07, 10.8, 22.47},
};
const float v5_2_harmonic_lna_level_offset = 0; // should be in correction table now -7; // Depends on where the transition to harmonic is done!!!!!! TODO find best frequency to transition to harmonic
@ -2447,7 +2447,7 @@ static const VNAShellCommand commands[] =
#ifdef ENABLE_COLOR_COMMAND
{"color" , cmd_color , CMD_RUN_IN_LOAD},
#endif
{ "if", cmd_if, CMD_WAIT_MUTEX | CMD_RUN_IN_LOAD },
{ "if", cmd_if, CMD_RUN_IN_LOAD },
#ifdef TINYSA4
{ "if1", cmd_if1, CMD_RUN_IN_LOAD },
{ "lna2", cmd_lna2, CMD_RUN_IN_LOAD },

@ -177,7 +177,8 @@ extern char *hw_text;
#define DRIVE2_MAX_FREQ 2100000000ULL // LO drive 2
#define LOW_SHIFT_FREQ 2000000ULL // shift IF to avoid zero Hz within IF
#define USE_SHIFT2_RBW 4000 // use shift2_level_offset if actual_rbw_x10 is larger then this.
#define USE_SHIFT2_RBW 8500 // shift2_level_offset rbw
#define USE_SHIFT1_RBW 6000 // shift1_level_offset rbw
#ifdef __NEW_SWITCHES__
#define DIRECT_START config.direct_start
#define DIRECT_STOP config.direct_stop

@ -4901,7 +4901,7 @@ again: // Spur redu
pureRSSI = Si446x_RSSI(break_on_operation);
if (LO_shifting && (signal_path != PATH_DIRECT)) {
if (f < 5000000)
pureRSSI += float_TO_PURE_RSSI(actual_rbw_x10>USE_SHIFT2_RBW ? config.shift2_level_offset : (lf < LOW_SHIFT_FREQ ? config.shift1_level_offset: 0.0));
pureRSSI -= float_TO_PURE_RSSI(actual_rbw_x10 == USE_SHIFT2_RBW ? config.shift2_level_offset : (actual_rbw_x10 == USE_SHIFT1_RBW ? config.shift1_level_offset : 0));
else
pureRSSI += float_TO_PURE_RSSI(config.shift_level_offset);
}
@ -6689,8 +6689,8 @@ float measure_jump(int i) {
right += actual_t[j];
}
right /= h_p;
if (i <= 1) // for 2MHz jump
return(right-left); // returns level jump low to high frequency.
// if (i <= 1) // for 2MHz jump
// return(right-left); // returns level jump low to high frequency.
return (left - right);
}
#endif
@ -7916,8 +7916,10 @@ void calibrate(void)
// setting.spur_removal = S_OFF;
// set_reflevel(-95);
} else if (i <= 1) {
if (i == 1)
set_RBW(8500);
if (i == 0)
set_RBW(USE_SHIFT1_RBW);
else
set_RBW(USE_SHIFT2_RBW);
set_refer_output(5); // 2MHz
setting.spur_removal = S_OFF;
} else {

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